TWA Flight 529

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TWA Flight 529
Lockheed L-049 Constellation, Trans World Airlines (TWA) JP7293287.jpg
A Lockheed L-049 Constellation of Trans World Airlines, similar to the accident aircraft
Accident summary
Date September 1, 1961
Summary Mechanical failure leading to loss of control
Site Willowbrook, DuPage County;
near Hinsdale, IL
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Passengers 73
Crew 5
Injuries (non-fatal) 0
Fatalities 78(all)
Survivors 0
Aircraft type Lockheed L-049 Constellation
Aircraft name Star of Dublin
Operator TWA
Registration N86511
Flight origin Boston, Massachusetts (BOS)
Stopover Chicago, Illinois (MDW)
Last stopover Las Vegas, Nevada (LAS)
Destination Los Angeles, California (LAX)

TWA Flight 529 was a Lockheed Constellation L-049 propliner, registration N86511, operating as a scheduled passenger service from Boston, Massachusetts to San Francisco, California. On September 1, 1961, at 02:05 CDT, the flight crashed shortly after takeoff from Midway Airport (ICAO: KMDW) in Chicago, killing all 73 passengers and five crew on board; it was at the time the deadliest single plane disaster in U.S. history.[1][2]

The accident was investigated by the Civil Aeronautics Board, which concluded its probable cause was the loss of a 5/16 inch bolt which fell out of the elevator control mechanism during the climb from Chicago, resulting in an abrupt pitch up followed by a stall and crash.[3][4]

Flight history

The four-engine propliner originated in Boston, and after making intermediate stops in New York and Pittsburgh, arrived at Chicago Midway Airport at 01:18 CST, where a new crew took over, and fuel and oil were added. At 02:00 the flight departed from runway 22, bound for Las Vegas, Nevada, the next stop. Five minutes later, while climbing westbound to 5,000 ft, the aircraft suddenly pitched violently upwards, resulting in an accelerated stall from which the crew was unable to recover. The aircraft crashed into terrain, and left a debris field of 200 by 1,100 feet.[3]

Investigation

Schematic of elevator boost linkage mechanism, showing location of missing bolt (A)

The CAB investigated the accident, and as the wreckage pieces were reassembled and scrutinized, it became apparent that a critical 5/16 inch AN-175-21 nickel steel bolt was missing in the elevator boost linkage mechanism.[5] By carefully examining and analyzing the various scuff marks and grease patterns near the missing bolt, the CAB investigators concluded that the bolt had fallen out prior to the aircraft's disintegration and collision with the ground, and not as a result of the accident itself. Without the bolt in place, the elevator (when in boost mode) and hence the entire aircraft would become uncontrollable, leading the investigators to deduce that the bolt had fallen out, most likely by working itself loose, a short time prior to the beginning of the accident sequence.[4]

The design of the Lockheed Constellation L-049 aircraft allowed the pilots to disable the hydraulic elevator boost and control the elevators manually via direct mechanical linkage. The pilots of the accident flight apparently attempted to revert to manual control as the aircraft began to pitch up, but the design was such that a continuous nose down pressure on the elevators made the shift to manual elevator control mechanically impossible.[6] Thus, according to the CAB's reconstruction of events, as the pilots were desperately applying nose down pressure to avoid a stall, they were also hampering themselves from shifting to manual mode and regaining elevator control.[4]

On December 18, 1962, the CAB published its final report on the accident, concluding that the probable cause was "... the loss of an AN-175-21 nickel steel bolt from the parallelogram linkage of the elevator boost system, resulting in loss of control of the aircraft."[4]

Aftermath

As a result of their investigation of the accident, the CAB urged the FAA to mandate a redesign of the elevator boost control, so that the shift to manual mode could be easily carried out by the pilots, even when applying nose down pressure. The FAA replied that they had asked the manufacturer to incorporate procedural changes in the aircraft's flight manual, but did not require any design changes.[4]

See also

External links

Notes

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  3. 3.0 3.1 Lua error in package.lua at line 80: module 'strict' not found.
  4. 4.0 4.1 4.2 4.3 4.4 Lua error in package.lua at line 80: module 'strict' not found. (Historical Aviation Accident reports, 1961, Trans World Airlines, PDF)
  5. Lua error in package.lua at line 80: module 'strict' not found.
  6. The actual wording from the CAB's final report is: "With the elevator at its maximum deflection (maximum hinge-moment or 40 degrees, depending on speed) and held there by full hydraulic pressure and with forward (nose-down) force on the column, it becomes difficult, if not impossible, to move the shift handle far enough to operate the shutoff and/or the bypass valves."